改进的喷射染色机上的深颜色还原染色棉布织物--外文翻译--纱线喷射染色控制系统设计.docx
《改进的喷射染色机上的深颜色还原染色棉布织物--外文翻译--纱线喷射染色控制系统设计.docx》由会员分享,可在线阅读,更多相关《改进的喷射染色机上的深颜色还原染色棉布织物--外文翻译--纱线喷射染色控制系统设计.docx(39页珍藏版)》请在淘文阁 - 分享文档赚钱的网站上搜索。
1、外 文 翻 译毕业设计题目: 纱线喷射染色控制系统设计 原文1:Deep-colour vat dyeing of cotton knit fabric on modified jet dyeing machine 译文1:改进的喷射染色机上的深颜色还原染色棉布织物 原文 2: Analysis of the factors influencing dye uptake on jet dyeing equipment 译文 2:喷射染色设备上影响染料吸收因素的分析 Deep-colour vat dyeing of cotton knit fabric on a modified jet dy
2、eing machineToday, cotton clothes are dyed with vat dyes in a continuous system, with stepwise operations of reducing the dye to leuco form, soaking the clothes in the bath under a nitrogen atmosphere, and then holding the clothes in an airatmosphere for oxidation. Soaping, washing, and application
3、of various auxiliary agents follow continuously to finish the processing.However, cotton knit fabric, which is not put into the continuous system because of its overstretching on the conveyor, must be vat dyed in a batch system, where inhomogeneous reduction and oxidation of the dyed fabric often le
4、ad to some defects in the product. This report describes a new method for stable vat dyeing of cotton knit fabric in a batch, especially deep-colour dyeing, using a modified jet dyeing machine operating without the use of nitrogen gas to purge oxygen.Before designing the mechanical system for deep-c
5、olour dyeing with vat dyes, which has not been practiced commercially until now, preliminary information on dye diffusion in cellulosic substrates was obtained using the cellophane film roll method, by which dye uptake at the surface and the diffusion behaviour of the dye within the roll were measur
6、ed quantitatively. As with other dyeing processes, it is desirable in vat dyeing that the temperature be as high as possible in order to reduce dyeing and processing time. However, increasing the temperature tends to result in unevenness in the dyed fabric, resulting in various defects in the produc
7、t. The dyeing conditions, including the concentrations of reducing agent, sodium hydroxide, and the weight ratio of used dye to fabric, were examined by test dyeing in an Erlenmeyer flask under a nitrogen atmosphere. The possibilities of lowering the liquor ratio, the dyeing temperature, and the dur
8、ation of each process were also examined in the flask experiment.The core technology for successful batch dyeing on a production scale consists in completely reducing the dye to leuco form for molecular dispersion in the dyeing liquor, preventing air penetration from outside into the reducing liquor
9、, making the contact of the knit fabric with the liquor as even as possible, exposing it gradually to overflowing water for gentle and homogeneous oxidation initially, and then completing the oxidation with the replaced oxidizing liquor. Any inhomogeneous contact of the fabric with the liquor leads
10、to faults such as spot stains due to contact with undispersed leuco dyes, streaking due to insufficient evenness of contact of the knit with the dyeing liquor and unlacing of the rope during circulation, and spread stains due to uneven oxidation.These problems are crucially serious in vat dyeing on
11、a jet dyeing machine. Rigorous airtightness is necessary. The speeds of the knit fabric and liquor circulation should be meticulously regulated, and the introduction of solutions of reducing agent and dye or oxidising agent into the dyeing liquor should be controlled so as to make the contact of the
12、 fabric with them as even as possible. To overcome these restrictions, necessary modifications to the dyeing machine are proposed in this study. In addition, monitoring of the redox potential and pH of the liquor in each process helps in following the progress of dyeing in situ and in making each op
13、eration controllable. These measurements are also useful in confirming the completion of processes of dyeing with leuco dyes and oxidation of the dyed fabric.The present study first reports preliminary investigations on dyeing in a Erlenmeyer flask and with the film roll method as a model for cotton
14、 knit dyeing. The measurements were performed for Indanthren Direct Black RB Coll.at 60, 70, and 80 C. Feasible conditions for stable production were established by referring to pre-examined data for each parameter, e.g. the concentration of reducing agent, sodium hydrosulfite and sodium hydroxide,
15、the liquor ratio of dyeing, and the oxidation process.Based on the data obtained by the Erlenmeyer test, the film roll method, and dyeing on the modified test jet machine for 12 kg of cotton knit fabric, reasonable operating conditions were established for vat dyeing on a 80 kg scale. Modifications
16、were made to the conventional jet dyeing machine to realise stepwise operations with the dyeing liquor, oxidation with water, and final oxidation with oxidising agent. After dyeing, soaping was carried out twice with foamless soap. We report that high quality of dyed fabric and reproducibility have
17、been attained consistently on the modified machine under production conditions for the past 2 years.ExperimentalMaterialsCotton knit fabric (30/1 cotton, 100% knit fabric, 24G-26 is the spec of a circular knittngmabhine. If the units are changed into cm unit, the number of needles, 9.49/cm (24G) and
18、 the diameter is 66.04cm (26) ) was purchased from Verite Co. Ltd, Japan. The fabric was scoured and bleached with hydrogen peroxide under standard conditions. Cellophane film of 0.043 mm thickness, supplied by Futamura Chemical Co. Ltd, Japan, was used after soaking in deionised water for 1 h at am
19、bient temperature.Dyes and chemicalsIndanthren Direct Black RB Coll. (CI Vat Black 9) was obtained from DyStar (Japan) and used as received. The structural formula is shown in Figure 1. Sodium hydrosulfite and sodium hydroxide were supplied by Wako Pure Chemical Industries, Ltd (Japan). Sodium meta-
20、benzene sulfonate (Ludigol) was purchased from BASF (Japan). A scouring agent (Neonol HT: ethylene glycol mono-n-butyl ether) and a softener (S-M1: alkylether X and potassium phosphate mixture) were supplied by Fushimi Chemicals Co. Ltd (Japan). Soaping, which was required to be foamless in the jet
21、dyeing machine, was carried out 2 times with a 1:1 mixture (by weight) of sodium tripolyphosphate and sodium meta-silicate. All the reagents were for production use. For the Erlenmeyer and the film roll expriments, deionised water was used, and for the production experiments, distilled water was use
22、d.Film roll methodSekido and Matsui were the first to report and give a full account of the cellophane film roll method to study the diffusion coefficients of some vat dyes . Figure 2 shows the assembly of the roll of cellophane film. The roll was put in a 50 ml solution containing 0.0056 g of the d
23、ye, 0.14 g of sodium hydroxide, and 0.1 g of sodium hydrosulfite in a test tube, and stoppered tightly under a nitrogen atmosphere. The tube was placed in a vibrator at 60, 70, and 80 C and shaken for 72 h. After dyeing, the rolled film was unrolled quickly, washed lightly with water, kept exposed t
24、o air for 1 h, and used for dye concentration measurement. Figure 3 shows the unrolled films. The absorbance at the maximum absorption wavelength (520 nm) for each film layer was measured on a UV-vis spectrophotometer (UV-2450; Shimadzu, Japan) for the dye concentrations of the respective layers. No
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